Characterization of the Anomalous Vibration Response of an Intentionally Mistuned LPT Rotor

被引:3
|
作者
Rodriguez-Blanco, Salvador [1 ]
Martel, Carlos [1 ]
机构
[1] Univ Politecn Madrid, Dept Matemat Aplicada Ingn Aeroespacial, Madrid 28040, Spain
基金
欧盟地平线“2020”;
关键词
turbomachinery aeroelasticity; bladed disk vibration; mistuning; FLUTTER;
D O I
10.3390/machines11010019
中图分类号
TM [电工技术]; TN [电子技术、通信技术];
学科分类号
0808 ; 0809 ;
摘要
The wind tunnel facility at the Centro de Tecnologias Aeronauticas was used to perform a set of experiments to study the effect of intentional mistuning on the forced response behavior of an aerodynamically unstable low-pressure turbine rotor. The intentional mistuning patterns were implemented by adding a small extra mass to some of the blades. The forced response of the rotor was therefore expected to show two resonance peaks with similar amplitudes, corresponding, respectively, to the vibration frequencies of the blades with and without added mass. However, on the post-processing of the measurements, some anomalous behavior was observed. Near resonance, the system response was synchronous with the forcing, and the frequency sweeps exhibited two resonance peaks, but it was found that the two peaks were clearly different, with the peak at lower frequency showing a much higher vibration amplitude than the high-frequency peak, and with some blades responding at both frequencies with a similar amplitude. In order to give a correct interpretation of the experimental results, a reduced-order model is derived that takes into account only the traveling wave modes coupled by the mistuning. This model, although extremely simple, is capable of reproducing the unexpected behavior of the experiments, and gives a clean explanation of the system response. It is shown that the relative size of the mistuning with respect to the frequency difference of the involved traveling-wave modes is the key parameter for the appearance of this phenomenon.
引用
收藏
页数:12
相关论文
共 50 条
  • [31] Identification of rotor bearing parameters using vibration response data in a turbocharger rotor
    Mutra R.R.
    Srinivas J.
    Journal of Computational and Applied Research in Mechanical Engineering, 2019, 9 (01): : 141 - 152
  • [32] Vibration response of coupled rotor systems with crack and misalignment
    Patel, T. H.
    Zuo, M. J.
    Darpe, A. K.
    PROCEEDINGS OF THE INSTITUTION OF MECHANICAL ENGINEERS PART C-JOURNAL OF MECHANICAL ENGINEERING SCIENCE, 2011, 225 (C3) : 700 - 713
  • [33] VIBRATION RESPONSE ANALYSIS OF MISTUNED BLADED DISK WITH UNDER-PLATFORM DAMPER: EFFECT OF VARIATION OF CONTACT CONDITION ON VIBRATION CHARACTERISTICS
    Kaneko, Yasutomo
    PROCEEDINGS OF THE ASME TURBO EXPO: TURBINE TECHNICAL CONFERENCE AND EXPOSITION, 2017, VOL 7B, 2017,
  • [34] Vibration response analysis of rotor system with initial thermal deformation
    Ma Y.
    Liu H.
    Deng W.
    Yang H.
    Hong J.
    Beijing Hangkong Hangtian Daxue Xuebao/Journal of Beijing University of Aeronautics and Astronautics, 2019, 45 (02): : 227 - 233
  • [35] Vibration response of rigid rotor in unloaded rolling element bearing
    Tomovic, Radoslav
    Miltenovic, Vojislav
    Banic, Milan
    Miltenovic, Aleksandar
    INTERNATIONAL JOURNAL OF MECHANICAL SCIENCES, 2010, 52 (09) : 1176 - 1185
  • [36] Study on vibration response reduction of bladed disk by use of asymmetric vane spacing (study on response reduction of mistuned bladed disk)
    Kaneko, Yasutomo
    Ohta, Masaki
    Mori, Kazushi
    Ohyama, Hiroharu
    International Journal of Gas Turbine, Propulsion and Power Systems, 2012, 4 (01): : 35 - 42
  • [37] The Amplification of Vibration Response Levels of Mistuned Bladed Disks: Its Consequences and Its Distribution in Specific Situations
    Chan, Y. -J.
    Ewins, D. J.
    JOURNAL OF ENGINEERING FOR GAS TURBINES AND POWER-TRANSACTIONS OF THE ASME, 2011, 133 (10):
  • [38] MISTUNED HIGHER-ORDER MODE FORCED RESPONSE OF AN EMBEDDED COMPRESSOR ROTOR, PART I: STEADY AND UNSTEADY AERODYNAMICS
    Li, Jing
    Aye-Addo, Nyansafo
    Kormanik, Nicholas, III
    Matthews, Douglas
    Key, Nicole
    Kielb, Robert
    PROCEEDINGS OF THE ASME TURBO EXPO: TURBINE TECHNICAL CONFERENCE AND EXPOSITION, 2017, VOL 7B, 2017,
  • [39] Study on transient vibration of bladed disk passing through resonance (transient response analysis of mistuned bladed disk)
    Kaneko, Yasutomo
    Hamaguchi, Taku
    Nihon Kikai Gakkai Ronbunshu, C Hen/Transactions of the Japan Society of Mechanical Engineers, Part C, 2013, 79 (801): : 1359 - 1371
  • [40] An Experimental Study on the Effects of Nonuniform Vane Spacing on Forced Response Reduction in a Mistuned Rotor Blisk in a Multistage Axial Compressor
    Leng, Yujun
    Dodda, Jhansi R.
    Key, Nicole L.
    JOURNAL OF TURBOMACHINERY-TRANSACTIONS OF THE ASME, 2025, 147 (02):