Design and characterization of the Sandia free-piston reflected shock tunnel

被引:5
|
作者
Lynch, K. P. [1 ]
Grasser, T. [2 ]
Spillers, R. [1 ]
Downing, C. [2 ]
Daniel, K. A. [1 ]
Jans, E. R. [2 ]
Kearney, S. [2 ]
Morreale, B. J. [1 ]
Wagnild, R. [1 ]
Wagner, J. L. [1 ]
机构
[1] Sandia Natl Labs, Aerosci Dept, Albuquerque, NM 87123 USA
[2] Sandia Natl Labs, Diagnost Sci Dept, Albuquerque, NM 87123 USA
关键词
Shock tunnel; Velocimetry; High enthalpy; DRIVER; FLOW;
D O I
10.1007/s00193-023-01127-4
中图分类号
O3 [力学];
学科分类号
08 ; 0801 ;
摘要
A new reflected shock tunnel capable of generating hypersonic environments at realistic flight enthalpies has been commissioned at Sandia. The tunnel uses an existing free-piston driver and shock tube coupled to a conical nozzle to accelerate the flow to approximately Mach 9. The facility design process is outlined and compared to other ground test facilities. A representative flight-enthalpy condition is designed using an in-house state-to-state solver and piston dynamics model and evaluated using quasi-1D modeling with the University of Queensland L1d code. This condition is demonstrated using canonical models and a calibration rake. A 25-cm core flow with 4.6-MJ/kg total enthalpy is achieved over an approximately 1-ms test time. The condition was refined using analysis and a heavier piston, leading to an increase in test time. A novel high-speed molecular tagging velocimetry method is applied using in situ nitric oxide to measure the freestream velocity of approximately 3016 m/s. Companion simulation data show good agreement in exit velocity, pitot pressure, and core flow size.
引用
收藏
页码:299 / 314
页数:16
相关论文
共 50 条
  • [21] HYPERSONIC TESTING IN VKI LONGSHOT FREE-PISTON TUNNEL
    RICHARDS, BE
    ENKENHUS, KR
    AIAA JOURNAL, 1970, 8 (06) : 1020 - &
  • [22] Establishment of steady separated flow over a compression-corner in a free-piston shock tunnel
    Mallinson, SG
    Gai, SL
    Mudford, NR
    SHOCK WAVES, 1997, 7 (04) : 249 - 253
  • [23] Design and modeling of a free-piston engine generator
    Wang, Jinlong
    Xiao, Jin
    Cheng, Yingdong
    Huang, Zhen
    FRONTIERS IN ENERGY, 2023, 17 (06) : 811 - 821
  • [24] DENSE GAS PHENOMENA IN A FREE-PISTON HYPERSONIC WIND TUNNEL
    ENKENHUS, KR
    PARAZZOL.C
    AIAA JOURNAL, 1970, 8 (01) : 60 - &
  • [25] Mass spectrometric measurements of the freestream composition in the T4 free-piston shock-tunnel
    Boyce, RR
    Takahashi, M
    Stalker, RJ
    SHOCK WAVES, 2005, 14 (5-6) : 359 - 370
  • [26] Mass spectrometric measurements of the freestream composition in the T4 free-piston shock-tunnel
    R. R. Boyce
    M. Takahashi
    R. J. Stalker
    Shock Waves, 2005, 14 : 359 - 370
  • [27] FREE-PISTON SHOCK-TUBE STUDY OF NITROGEN DISSOCIATION
    KEWLEY, DJ
    HORNUNG, HG
    CHEMICAL PHYSICS LETTERS, 1974, 25 (04) : 531 - 536
  • [28] A Review of the Design and Control of Free-Piston Linear Generator
    Wang, Xuezhen
    Chen, Feixue
    Zhu, Renfeng
    Yang, Guilin
    Zhang, Chi
    ENERGIES, 2018, 11 (08):
  • [29] Hybrid controller design of a free-piston energy converter
    Pang, Yan
    Xia, Hao
    INTERNATIONAL JOURNAL OF APPLIED ELECTROMAGNETICS AND MECHANICS, 2014, 46 (04) : 751 - 762
  • [30] Mass spectrometric measurements of driver gas arrival in the T4 free-piston shock-tunnel
    Boyce, RR
    Takahashi, M
    Stalker, RJ
    SHOCK WAVES, 2005, 14 (5-6) : 371 - 378