A case study of rupture in overhead ground wire twined by armor rod

被引:0
|
作者
Deng, Honglei [1 ]
Peng, Ruidong [1 ]
Zhong, Meishan [1 ]
Yang, Rui [2 ]
Liang, Yongchun [3 ]
Guo, Deming [1 ]
Liu, Gang [1 ]
机构
[1] School of Electric Power Engineering, South China University of Technology, Guangzhou,Guangdong,510640, China
[2] Dongguan Power Supply Bureau of Guangdong, Power Grid Co., Ltd., Dongguan,Guangdong,523008, China
[3] Electric Power Research Institute of Guangdong Power Grid Co., Ltd., Guangzhou,Guangdong,510080, China
基金
中国国家自然科学基金;
关键词
Armor - Wire - Structural optimization - Accidents;
D O I
暂无
中图分类号
学科分类号
摘要
The armor rod (AR) is used to repair the damaged overhead ground wire (OGW) and prevent the wear of the OGW in the suspension clamp in engineering. Once the OGW at the AR terminal breaks, it may lead to temporary blackout, which also causes the severe economic losses, or even threatening public safety. However, there are few literature or report about this type of accident at present. Therefore, based on a rupture accident of OGW at the AR terminal, the reason for this accident was investigated in this paper. Firstly, the description of the accident background and the material analysis for the accident sample were presented to preliminarily determine the damage characteristics of OGW and the cause of the accident. Secondly, simulation experiments for the transient temperature rise of the AR terminal were conducted. The macroscopic morphology characteristics of the experimental samples were also analyzed. Finally, based on the electromagnetic thermal coupling, a finite element model of the AR terminal of OGW was established. The overheating mechanism at the AR terminal was also discussed according to the model. The discharge occurrs at the AR terminal under the short-circuit current (SCC), and it is also the prime factor that causes the high temperature of OGW. The research methods and conclusions in this paper can provide theoretical guidance for the analysis of similar accidents and the optimization design of structures. © 2021 Elsevier Ltd
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