Study and Pilot Test of Multiple Thermal-Fluid Stimulation in Offshore Nanpu Oilfield

被引:0
|
作者
Han, Xiaodong [1 ,2 ]
Zhong, Liguo [1 ]
Liu, Yigang [3 ]
Zou, Jian [3 ]
Wang, Qiuxia [3 ]
机构
[1] China Univ Petr, Beijing, Peoples R China
[2] CNOOC, Beijing, Peoples R China
[3] CNOOC, Tianjin Branch, Tianjin, Peoples R China
来源
SPE PRODUCTION & OPERATIONS | 2020年 / 35卷 / 03期
关键词
HEAVY OIL; STEAM INJECTION; RECOVERY; RESERVOIRS; BEHAVIOR; WELLS;
D O I
暂无
中图分类号
TE [石油、天然气工业];
学科分类号
0820 ;
摘要
Heavy-oil resources whose underground oil viscosity is greater than 350 mPa.s is abundant in the Bohai oilfield. Because of the lack of effective exploitation technology, production performance with cold-production methods was not satisfactory. Seeking an effective method of heavy-oil exploitation, the multiple thermal-fluid stimulation was proposed and studied, in which hot water or steam mixed with carbon dioxide (CO2) and nitrogen (N-2) would be injected into the formation for heating the oil and improving heavy-oil production. Considering the limitation of the offshore platform, a miniaturized multiple thermal-fluid generator was designed and developed. Integrated technologies such as seawater desalinization, heat insulation, and anticorrosion methods were also studied and developed. A pilot test of multiple thermal-fluid stimulation was conducted in Nanpu oilfield, starting in 2008. Until now, the pilot test has lasted for more than 10 years, and a total of 27 cycles of multiple thermal-fluid stimulation have been carried out. The oil-production rate and periodic-oil production amount of the thermal wells were both greatly improved. The cumulative oil produced by multiple thermal-fluid stimulation reached approximately 5.7 x 10(5) m(3), and the incremental oil production is approximately 2.6 x 10(5) m(3). The performance of oil production was satisfactory. As the first offshore thermal pilot area, the application experience showed that multiple thermal-fluid stimulation was effective for exploitation of heavy oilfields. With the increase of the stimulation cycles, a gas-channeling problem emerged and resulted in a decrease in the oil-production rate. New methods need to be studied and used for further enhancing oil recovery in Nanpu oilfield at the late stage of multiple thermal-fluid stimulation.
引用
收藏
页码:592 / 603
页数:12
相关论文
共 50 条
  • [1] Study and pilot test of multiple thermal-fluid stimulation in offshore nanpu oilfield
    Han X.
    Zhong L.
    Liu Y.
    Zou J.
    Wang Q.
    SPE Production and Operations, 2020, 35 (03): : 592 - 603
  • [2] Pilot test of horizontal drilling and completion techniques in Nanpu Oilfield
    Zhu, Kuanliang
    Feng, Jinghai
    Han, Fei
    Li, Nan
    Shiyou Kantan Yu Kaifa/Petroleum Exploration and Development, 2009, 36 (05): : 658 - 663
  • [3] Recovery Method and Parameter Optimization of a Pilot Test for Conformance Control Flooding and Thermal Recovery in the Offshore Heavy Oilfield
    Zhou, Yanxia
    Lu, Xiangguo
    Cao, Bao
    Liu, Yigang
    Zhang, Yunbao
    Zhong, Xun
    GEOFLUIDS, 2021, 2021
  • [4] Thermal-fluid and electromagnetic coupling analysis and test of a traction motor for electric vehicles
    Chang, Hao-Yen Howard
    Yang, Yee-Pien
    Lin, Frank Kou-Tzeng
    JOURNAL OF THE CHINESE INSTITUTE OF ENGINEERS, 2018, 41 (01) : 51 - 60
  • [5] Thermal-fluid flow analysis and demonstration test of a spent fuel storage system
    Lee, J. C.
    Choi, W. S.
    Bang, K. S.
    Sea, K. S.
    Yoo, S. Y.
    NUCLEAR ENGINEERING AND DESIGN, 2009, 239 (03) : 551 - 558
  • [6] Nonintrusive and Multidimensional Optical Diagnostics and Their Applications in the Study of Thermal-Fluid Systems
    Ma, Lin
    HEAT TRANSFER ENGINEERING, 2016, 37 (3-4) : 359 - 368
  • [7] Study on thermal-fluid effect of thermal energy storage tank design in solar energy applications
    Ali, Tanti
    Abu Bakar, Rosli
    Sup, Billy Anak
    Zainudin, Mohd Farid
    Ming, Gan Leong
    2ND INTERNATIONAL CONFERENCE ON SUSTAINABLE ENERGY ENGINEERING AND APPLICATION (ICSEEA) 2014 SUSTAINABLE ENERGY FOR GREEN MOBILITY, 2015, 68 : 3 - 11
  • [8] Temperature Rise Test and Thermal-Fluid Coupling Simulation of an Oil-Immersed Autotransformer Under DC Bias
    Li, Mingyang
    Wang, Zezhong
    Zhang, Junshuang
    Ni, Zhengze
    Tan, Ruijuan
    IEEE ACCESS, 2021, 9 : 32835 - 32844
  • [9] Computational Thermal-Fluid Dynamics analyses of borated water distribution in the Vacuum Vessel of the Divertor Tokamak Test facility
    Bonifetto, Roberto
    Barone, Gianluca
    Dalla Palma, Mauro
    Froio, Antonio
    Martelli, Emanuela
    Vair, Federico
    Zanino, Roberto
    Zappatore, Andrea
    FUSION ENGINEERING AND DESIGN, 2024, 202
  • [10] Experimental Study on Convective Thermal-Fluid Flow Transport Phenomena in Circular Tube Using Nanofluids
    Torii, Shuichi
    Satou, Yutaka
    Koito, Yasushi
    INTERNATIONAL JOURNAL OF GREEN ENERGY, 2010, 7 (03) : 289 - 299