Analysis of R Bank Frequent Action Problem in Yangjiang Nuclear Power Plant

被引:0
|
作者
Xiang H. [1 ]
Liu Y. [1 ]
Huang Z. [1 ]
Chen J. [1 ]
Chen K. [1 ]
机构
[1] State Key Laboratory of Nuclear Power Safety Monitoring Technology and Equipment, China Nuclear Power Engineering Co. Ltd., Shenzhen, 518124, Guangdong
来源
关键词
Differential; First-order inertia; Lead lag; R bank;
D O I
10.13832/j.jnpe.2019.01.0097
中图分类号
学科分类号
摘要
In the 2nd and 3rd nuclear fuel cycles of Unit 1,Unit 2 and Unit 3 in Yangjiang Nuclear Power Plant,, R bank acts frequently, seriously affecting the safety with operation of the unit. In this paper, the logic control principle of R bank and the loading of core are analyzed, and the transfer function of first-order inertia, lead lag and differential link is converted into difference equation. The theoretical calculation is carried out before the parameter is modified, and the temperature ±4℃ disturbance simulation test upon 87%FP power platform is carried out on the plant simulator. The test results show that the modified parameters are correct and can solve the frequent action problem of R bank. After the modification of the parameters for Unit 2, the R bank acts normally, and R bank action frequency is about 1 time per 2 days. © 2019, Editorial Board of Journal of Nuclear Power Engineering. All right reserved.
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页码:97 / 100
页数:3
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